Volume 33 Issue 3
May  2016
Turn off MathJax
Article Contents
HOU Yue, BAN Shijun, ZHAO Yunlong. Modified Natural Polymer Drilling Fluid Used in Exploration Wells in the Gulf of Liaodong[J]. DRILLING FLUID & COMPLETION FLUID, 2016, 33(3): 60-63. doi: 10.3969/j.issn.1001-5620.2016.03.012
Citation: HOU Yue, BAN Shijun, ZHAO Yunlong. Modified Natural Polymer Drilling Fluid Used in Exploration Wells in the Gulf of Liaodong[J]. DRILLING FLUID & COMPLETION FLUID, 2016, 33(3): 60-63. doi: 10.3969/j.issn.1001-5620.2016.03.012

Modified Natural Polymer Drilling Fluid Used in Exploration Wells in the Gulf of Liaodong

doi: 10.3969/j.issn.1001-5620.2016.03.012
  • Received Date: 2015-11-22
  • Publish Date: 2016-05-31
  • The well DS4 is an areal exploration well located in the offshore Gulf of Liaodong in the north Bohai Sea. The well DS4, a long open-hole well, penetrated formations with complex geology and many oil and gas bearing zones. Based on the studies on the inhibitive capacity and plugging capacity of the drilling fluid, as well as reservoir protection mechanism, a modified natural polymer drilling fluid was optimized. The results of the laboratory experiments have revealed that the inhibitive capacity and the plugging capacity of the drilling fluid are greatly enhanced after treatment with the strong shale inhibitor AP-1 and the plugging agent DLP. Using this modified natural polymer drilling fluid, mud losses previously occurred in drilling the highly permeable Minghuazhen formation and Guantao formation were minimized, and the borehole wall instability in drilling the lower Dongying formation (shales) was brought under control with lower mud weights, realizing safe and fast drilling. This drilling fluid has good lubricity; in the second interval, which has length of 3,131 m, horizontal displacement of 1,060 m and well angle of 34.5℃, the wireline logging was 100% successful, with no repetition. The drilling fluid has low fluorescence, which is helpful in pinpointing pay zones accurately. The drilling fluid has good reservoir protection ability; the well DS4 had good oil shows, and high production rate was obtained during well testing.

     

  • loading
  • 胥思平,沈忠厚,丁海峰,等. 天然高分子钻井液体系的研究与应用[J]. 钻井液与完井液,2006,23(6):33-37. XU Siping, SHEN Zhonghou, DING Haifeng, et al. Research and application of natural polymer drilling fluid[J]. Drilling Fluid &Completion Fluid,2006,23(6):33-37.
    王睿,马长光.环保型天然高分子水基钻井液的研究与现场应用[J]. 精细石油化工进展,2009(12):15-18. WANG Rui,MA Changguang.Research and field application of environmental natural polymer water base drilling fluid[J]. Advances in Fine Petrochemicals,2009(12):15-18.
    郑力会. 改性天然高分子基钻井液流变性研究[J]. 石油天然气学报(江汉石油学院学报),2007(6):101-103. ZHENG Lihui. Rheology research of natural polymer drilling fluid[J]. Journal of Oil and Gas Technology (Journal of Jianghan Petroleum Institute),2007(6):101-103.
    王树永. 铝胺高性能水基钻井液的研究与应用,钻井液与完井液,2008, 25(4):23-25. WANG Shuyong. Research and application of Aluminum amine high performance water-based drilling fluid[J]. Drilling Fluid & Completion Fluid,2008, 25(4):23-25.
    孙德军,王君,王立亚,等. 非离子型有机胺提高钻井液抑制性的室内研究[J]. 钻井液与完井液,2009, 26(5):7-9. SUN Dejun, WANG Jun,WANG Liya,et al. Indoor research on the improvement of the drilling fluid inhibition by non ionic organic amine[J]. Drilling Fluid & Completion Fluid, 2009,26(5):7-9.
  • 加载中

Catalog

    通讯作者: 陈斌, bchen63@163.com
    • 1. 

      沈阳化工大学材料科学与工程学院 沈阳 110142

    1. 本站搜索
    2. 百度学术搜索
    3. 万方数据库搜索
    4. CNKI搜索

    Article Metrics

    Article views (570) PDF downloads(200) Cited by()
    Proportional views
    Related

    /

    DownLoad:  Full-Size Img  PowerPoint
    Return
    Return