Volume 33 Issue 3
May  2016
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WANG Maogong, XU Xianguang, SUN Jinsheng, WANG Lihui, YANG Haijun, WANG Baocheng. Study and Application of Additives for Synthetic Fluids with GTL as the Base Fluid[J]. DRILLING FLUID & COMPLETION FLUID, 2016, 33(3): 30-34,40. doi: 10.3969/j.issn.1001-5620.2016.03.006
Citation: WANG Maogong, XU Xianguang, SUN Jinsheng, WANG Lihui, YANG Haijun, WANG Baocheng. Study and Application of Additives for Synthetic Fluids with GTL as the Base Fluid[J]. DRILLING FLUID & COMPLETION FLUID, 2016, 33(3): 30-34,40. doi: 10.3969/j.issn.1001-5620.2016.03.006

Study and Application of Additives for Synthetic Fluids with GTL as the Base Fluid

doi: 10.3969/j.issn.1001-5620.2016.03.006
  • Received Date: 2016-01-09
  • Publish Date: 2016-05-31
  • To improve the high temperature rheology and filtration property of the synthetic base drilling fluid using gas-to-liquid (GTL) oil as the base fluid, an organophilic clay having superior gel properties and an environmentally friendly filter loss reducer made from natural humic acid, have been developed. A GTL base drilling fluid was formulated with the organophilic clay, the modified humic acid, a primary emulsifier and secondary emulsifier previously developed. The organophilic clay, DR-GEL, was made by intercalating dihexadecyl dimethyl ammonium chloride into the crystal layers of a purified sodium montmorillonite, and had good gel performance in GTL (percentage of colloid particles to 98%), high viscosity and gel strength (3 Pa), and good high temperature stability (it functioned at 220℃)in laboratory experiments. The filter loss reducer, DR-FCLA, was made by modification of purified humic acid with dihexadecyl dimethyl ammonium chloride and diethylene triamine. DR-FCLA greatly reduced the HTHP filter loss, helped make the drilling fluid emulsified better and improved the rheology of drilling fluid. It functioned at high temperatures up to 230℃. The synthetic drilling fluid made with these additives had densities ranging in 1.6-2.3 g/cm3, good rheology (AV=27-61 mPa·s, YP=6-9 Pa) at temperatures ranging in 120-200℃, high electrical stability (ES>800 V), and HTHP filter loss <2.5 mL. This synthetic drilling fluid has been successfully used in Sumatra, Indonesia to drill the well NEB Basement-1 in Block Jabung. The properties of the drilling fluid remained stable for 40 days at bottom hole temperatures higher than 180℃. Difficulties in maintaining the suspension and cuttings carrying capacity of drilling fluid have been solved since then.

     

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